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Net additional production over seven months is more than 1,550 BOE (20:1)
Details
- Permian Basin: drilled in 1959, completed into the Wolfcamp in 2006
- Well Type: vertical/unfrac’d
Treatment
- Treated with 1,500 gallons of nanoActiv® HRT in May 2018
Results
- Oil production stabilized around 9 bbld for the first 5 months after treatment and around 8 bbld after seven months.
- Gas has fluctuated between 80-90 MCFD on average post-treatment.
- Water production continuing to decline after initial spike.
Daily oil production has sustained more than double BOPD for 7 months post-treatment and counting.